May 272016
 

The opportunity to go travelling for six months, neatly avoiding the whole of the UK winter, was too good to miss! The finishing line of the long running restoration was tantalisingly in sight, with only a few minor trimming tasks to complete before taking the car up to Suffolk & Turley to have the hood fitted.

The final few months of last summer was spent desperately trying to arrange for the hood to be fitted but circumstances were against me and time ran out. Still it’s a good excuse for yet more gratuitous holiday snaps to explain the lack of progress:

  • Che Guevara, Plaza de la Revolución Havana

While travelling, I had at least managed to come to an agreement for Suffolk & Turley to schedule the hood to be fitted towards the end of May. I would take the hood frame up as soon as I returned to the UK at the start of May so they could address the canopy issues. The car would follow a two weeks later to have the hood fitted at their workshop, weather permitting!

It will have been a long time coming, the car has been hoodless for almost a year since it was MOT’ed. The two weeks would give me enough time to complete the few other trimming jobs beforehand. Suffolk & Turley had suggested leaving off the door cards and a few of the vinyl-covered metal panels as it’s best to fit them after the trimming of the hood.

I was pondering whether to fit the chrome hardtop mounting brackets as they might get in the way while fitting the hood. These brackets have a Tenax fastener stud for securing the hood envelope. As the envelope was missing when I got the car, I became side-tracked trying to understand how the envelope fitted over a lowered hood.

Tenax stud on hardtop mounting bracket Operating manual show stud positions

It then dawned on me that I’d forgotten to fit the other two Tenax studs which are mounted on the rear bulkhead to attach the hood envelope straps. The studs pass through the bulkhead vinyl and are secured by a nut and washer within the boot space. The realisation soon turned to a sinking feeling – getting out of this pickle was a cyclical conundrum of my own making.

Spot the deliberate mistake
(no – not the missing seat!)
These tiny Tenax studs should have
been fitted through the bulkhead Hardura

I had spent some time trying to make the installation of the inertia reel seat belts as neat as possible … and I must admit I was quite pleased with the outcome. However it had now come back to haunt me. Needing to retro-fit the studs had created quite a dilemma. It was now impossible to locate the holes for the studs in the bulkhead since it and the boot space had now been covered with Hardura.

The only option was to remove the Hardura trim in the boot to reveal the mounting holes. However I had mounted the seat belt inertia reels over the boot trim in my quest for neatness. So the reels would have to be removed before the Hardura. However the removal of each inertia reel is via a single bolt passing through the bulkhead from the cabin. Again the bolt heads had been covered by the bulkhead Hardura to keep everything neat and tidy.

Inertia reels were mounted
over the boot Hardura trim
… and secured by bolts which
were then hidden under Hardura

Therefore I would also have to remove the bulkhead Hardura too … but I needed the bulkhead Hardura in place to mount the studs!!! Hmmmm ….

After some thought, a plan was hatched to lift as little as possible of the bulkhead Hardura. Just enough to provide access to the bolt heads. The difficulty was the studs are located quite close to the inertia reel mounting bolts. In addition, I’d been rather diligent in making sure the bulkhead Hardura had been well and truly stuck down in the first place.

The internet can be a wonderful source of information at times and a suggestion was to use Zippo lighter fuel to weaken the contact adhesive’s bond. This worked a treat and had the benefit of not damaging either the Hardura or paint work and evaporated fairly quickly.

Bulkhead Hardura was carefully lifted Lighter fuel reduces contact adhesive bond Both boot Hardura & Dynaliner were trashed

Although it was a very slow and messy job. One that I hope never to repeat! The lighter fuel slowly dissolved the contact adhesive which enabled various implements and fingers to lift the Hardura without pulling off the jute backing. However it soon evaporated causing said fingers to stick together and to anything else they came in contact with. The reinforced tape used to cover the anti-drumming/strengthening indentations was a great help in lifting the trim and enabled large areas to be lifted quite easily.

Unfortunately the same could not be said for the trim in the boot. Both the Hardura and Dynaliner underlay were destroyed when they were removed. Fortunately I had enough left over of both to re-trim the boot. I decided to repeat my ‘tidy’ installation because the lifting of the trim, whilst messy, hadn’t been as bad as I had feared.

So the order of re-fitting was:

  • Fit the two Tenax studs to the bulkhead!
  • Re-trim the boot Dynaliner and biscuit coloured Hardura
  • Fit the boot side boards and mount the inertia reels
  • Stick down the lifted bulkhead Hardura
  • Refit the seat belt webbing and boot release cable

Once the boot trim had been removed, a needle was pressed through the holes for the studs to indicated their positions from the cabin side. A drill bit rotated by hand was sufficient to create the necessary hole in the layers of trim into order to fit the studs. With the Dynaliner in place, the Hardura was bonded to it with spray contact adhesive. I found it easier to bond the middle third first before tackling each end.

Position of Tenax stud located! Dynaliner fitted and masked for bonding

After the inertia reels were bolted in place, the top of the bulkhead was re-covered with the reinforced tape. This was initially done to stop the indentations showing through over time but has the added benefit of making the trim removal easier in future. Heaven forbid!

Plenty of reinforced tape was laid down before bonding the lifted section of Hardura

The seat belt webbing was then fed through the bulkhead and connected to the inertia reel. It’s not a job I enjoyed as it’s fiddly, hard to get at and there’s a potential to ruin the reels. The spring in the reel has to be at it’s most coiled state when the end of the webbing is fed through the centre of the reel. There’s a real risk of accidentally letting go of the centre which needs to be held against the spring pressure. If it’s allowed to uncoil freely then the spring becomes unseated and breaks the internal mechanism which is sealed.

Laying out webbing to avoid kinks Apart from a final clean, all sorted

After rectifying the stud problem it was rather disappointing to find out that they still can’t take the car to fit the hood. It has now been delayed until the start of June. At times I wonder if it will ever have a hood!

May 162016
 

The trimmers, Suffolk & Turley, suggested that it would be useful to trial fit the hood frame before bringing the car up to fit the soft top. The only two adjustments I could find were moving the mounting brackets fore and aft and adding shims underneath the bracket to raise the frame away from the body. So it shouldn’t be too difficult …. I really should know better by now!

Parts problems
S & T had inspected the hood canopy and condemned it to the scrapheap but, by chance, Martin Robey had just one remaining in stock. It was purchased on the spot to avoid any further delays, despite the eye-watering cost. When it failed to turn up several days later Robeys received a chase up call. It was only then that they admitted they didn’t actually have any in stock. It would be several weeks before a new batch were manufactured. The new canopy eventually finally turned up some two months later. It was very frustrating, although worse was to come …!

The ‘complete’ hood frame bolt set (SBS9069) from SNG Barratt wasn’t much better! The one thing you could say about it, it was anything but complete! Some smaller washers didn’t fit any of the bolts in the kit and all the brass washers (2x BD541/22 & 2x BD541/23) were missing for the pivot joint between the links and the front canopy.

Their bolt set appears to be just for the parts to attach the folding links to the hood frame sticks. The four ‘special’ bolts and brass washers securing the frame to the chassis need to be purchase separately; the bolts pivoting the main sticks (BD19160) and the bolts fixing the control link to the chassis body (BD19393).

The SNG website suggests 8 brass washers (BD541/30) are required for these four special bolts. However the bolts have different diameters, so I found it required only four of these larger washers for the pivot joint for the main sticks. The control link bolts require four of the smaller washers, BD541/23.

To be fair to SNG Barratt, the parts of their website had been taken from a parts lists produced by a third party which I suspect is incorrect. SNG even supplied the missing/incorrect pieces free of charge which was a nice gesture. However the toing and froing added yet more unwelcome delays.

Trial fitting the hood frame
The first task was to loosen the various pivot points in the frame links which had been locked in position by the powder coating and re-tap all the screw threads. A sharp blade was sufficient to break the paint seal on the joints to allow a light oil to be worked in, until they were well lubricated and operating smoothly.

The hood sticks pivot on the special bolts which pass through the chassis mounting brackets. It was a tight squeeze inserting the brass washers that sit either side of the pivot points to aide rotation. A screwdriver was needed to prise open the brackets to insert the second washer. Fortunately the bolt has a tapered shoulder which helps pull the final washer into alignment.

Shouldered pivot bolt screws
Note: lubrication hole for pivot joint
Two brass washers are fitted per side.
Brackets are handed & bolt heads face inwards
So far so good – the hood sticks fitted! Shims may be needed under B-post brackets

The two folding mechanisms (or links) are attached to the hood sticks by two bolts each side. A further bolt secures their control link arm to the chassis, on inside of the B-post. Again brass washers are fitted to each joint. One thing I’ve noticed on most cars is the control link arms rub against the vinyl covered B-post trim, causing unsightly wear damage. When I have more time, I plan to investigate whether a spacer can be fitted, to lift the control link away from the trim.

The cantrails are simply bolted to the folding mechanisms and don’t have any adjustability.

Folding mechanism in place Cantrails and canopy link added

A watertight seal between the hood and drop glass (don’t laugh!) is created by sections of rubber moulding attached around the cantrails and the vertical main pillar posts. A lip to receive the rubber is created by small angled brackets which are just riveted to the cantrails (the lip is integral to the main pillar pieces).

There was some evidence that these brackets had been repositioned as there were several sets of drilled holes. I had assumed this was to fine tune their alignment with the drop glass. However, rather oddly, only one set of holes matched those in the cantrail. So I’m a bit mystified what had gone on in the past. I do know, from the bodging of the canopy, the hood has been apart at some stage.

Riveting brackets to cantrail rubbers

The range of travel of the canopy is limit by a stop stud attached to the link mechanisms. From the closed hood position, the front of the canopy can be raised slightly, until the stop studs are reached. At which point, pushing the canopy further up causes the link mechanisms to start folding.


New & old hood stop studs

Unfortunately both studs were rusted firmly in place and so the only option was to carefully cut each nut off with a Dremel. The remains of the studs were then used as a pattern in fabricating replacements in stainless steel.

The studs have clearly been designed to allow for a small degree of adjustability because the threaded section is not concentric with the main body of the stud. Rotational adjustment is made via the screwdriver slot. I’ve not been able to work out why this is needed.

Finally the hood canopy was fitted. As the strengthening wood bow still needs to be fettled to fit the canopy, it was only possible to fit the outer two hood retaining clamps at this stage. The fit of the brand new Robey canopy was truly shocking. It wasn’t even close.

The curvature of the front of the canopy is all wrong. The front centre section bends downwards too much so it is in hard contact with the windscreen chrome when the clamps are engaged. Also the outside corners protrude too far and there’s a substantial gap to the same chrome trim. I’ve had trouble with some replacement parts but this is about as worse as it gets.

The new Robey canopy fitted Fit along windscreen is atrocious
Daylight through the gap Each side also protrudes too far

The fit is so poor I had to abandon thoughts of completing the trial fitting and called Suffolk & Turley to discuss my options. It will take extensive sheet metal work to rectify. Fortunately RS Panels are next door to S&T. They will be asked to undertake the panel work to obtain a good fit before the trimming of the hood canvas.

It was not the first time they had come across this problem with Robey canopies. Something that really shouldn’t be necessary on a new panel, especially when charged such an extortionate price. I suspect they just churn them out thinking if they look about right they’ll have got away with it. By the time the customer finds out, it will probably be too late. There’s no excuse for it.

The impact was that it hadn’t been possible to have the hood fitted before heading off travelling for six months. I had hoped to arrange for the hood work to be done while I was abroad, so I could return to a completed car. However the logistics and available slots in people’s calendars meant it wasn’t to be.